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A Saturday press conference equipped staunch a short replace from the National Transportation Safety Board touching on the aviation incident on Thursday morning that claimed the lives of NASCAR driver Greg Biffle, his family, and three others.
By Friday, the NTSB had formally begun its investigation into the incident that came about on the Statesville Regional Airport nonetheless had scant information as preliminary interviews and records acquisition had staunch started.

NASCAR CupInvestigation timeline into lethal Greg Biffle airplane wreck released

NASCAR CupNASCAR story Greg Biffle and family killed in airplane wreck
That modified into largely the theme of a Saturday morning replace performed, over as soon as more by Board Member Michael Graham and Investigator-In-Cost Dan Baker.
“We peaceable attain now not know the conditions which led the airplane … to attempt and return to the airport,” Graham said in an opening commentary. “But that is the level of passion of our investigation.”
However, Graham did verify a text message change that came about between Cristina Grossu Biffle, the wife of the susceptible NASCAR massive name and her mom, which had been previously reported on Thursday.
Cathy Grossu told CBS on Friday that she modified into texted merit and forth alongside with her daughter that morning.
“Then she said something like ‘We’re in trouble, emergency landing.’ And I texted back, ‘What’s wrong with the plane?'” Grossu told the community. “Then the next thing was (the SOS alert) that you get from your automatic Apple phones when you have an accident or something. And so I knew that something was wrong.”
On Friday, Graham said he wasn’t responsive to that message and asked for additonal information from these with firsthand records and got it between press conferences.
“This morning, I will verify that the NTSB is responsive to 1 short text message from a passenger aboard the airplane to a family member that read ‘emergency landing’ (nonetheless) we’re now not responsive to any various communications from passengers on board the airplane to these on the bottom,” Graham said.
Graham added that the NTSB peaceable isn’t definite who modified into the pilot for the 10 minutes between rob-off and the failed emergency return to the airport.
Biffle modified into a licensed pilot as had been Dennis and Jack Dutton. Also on the airplane had been Biffle’s 14-year-susceptible daughter Emma (with first wife Nicole Lunders), 5-year-susceptible son Ryder and long-time NASCAR everyman Craig Wadsworth.
“I attain now not beget any extra records about who modified into within the left seat on the time,” Graham said. “We attain now stay wide awake for that every the records about all of the pilot rated occupants will be integrated in our preliminary picture.”
That is expected to advance merit inner 30 days even supposing the best prognosis from the agency will rob 12 to 18 months to total.
Graham said the NTSB has a level of self assurance who the pilot modified into nonetheless needs to envision that before publishing.
“At this point, we have a lot of really good information,” Graham said. “We’re fairly confident with the left seat occupant but we need to verify that. We need to be accurate in what we do. And from a survival standpoint, which is part of what we investigate, we want to know where everyone was sitting and that is a little more difficult in a crash like this.”
Within the 12 hours between the two press conferences, Graham said the NTSB has performed more than a few ogle statements and are validating the evidence procured. “Early indication from extra than one sources point out that the airplane modified into real on approach, configured for landing with the landing lights on,” Graham said. “However the airplane modified into coming in low. “That records is per the debris discipline our crew continues to glance and is per the first aspects of affect on the airport runway gentle stanchion located approximately 1800’ from the runway threshold.” However, Graham added that there might be sufficient technical evidence to search out out why that modified into the case. “It did look like the aircraft was configured properly for landing but it was low in the videos,” Graham said. “But we have no other indication over what went wrong at this time.” Since Friday morning’s replace, the NTSB has documented the debris discipline, airplane wreckage conditioning, negate locations and flight controls. The flight boom recorder modified into transported to NTSB headquarters in Washington, D.C. and the records is attempting to be recovered by consultants. Amongst the objects serene from the debris for prognosis: “All of these are being sent to NTSB recorders labs in Washington, D.C.,” Graham said. “We can select whether or now not records and relevant records would be recovered from these objects.” Graham said these will show essential in figuring out most seemingly reason. The NTSB also got the upkeep log and would perchance perchance well impartial spend all of this records to search out out the burden and balance and affect load. Both engines beget been analyzed and a drone modified into in a space to derive airborne on Friday amidst a indubitably windy day nonetheless modified into now not in a space to total that work unless Saturday morning as soon as instances calmed down.
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